| Authors |
Michael Runtuwene,SPE, Muhammad Hilmi Fasa,SPE, Fitria Dewi Rachmawati,SPE,
Muhammad Wijanarko,SPE, Arief Kadarsyah,JOB Pertamina – Medco E&P Tomori
Sulawesi; Novi Komalasari,SPE,Nuratas Gurnito,Halliburton
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Abstract
Matrix acidizing has been a successful stimulation method to enhance
production in carbonate reservoirs. One of the challenges is to distribute the
acid evenly along the interest zone to achieve a maximum stimulation effect,
due to the differences in porosity, permeability and degree of damage along the
interest zone.
Well-S delineation gas well, located in Senoro Field Sulawesi-Indonesia, is
drilled through a carbonate reservoir. It was decided to use an acid soluble
diversion agent instead of conventional proppant. This diversion agent is an
acid system that contains a polymer that crosslinks as the acid spends to near
completion, with this crosslink then disappearing as the acid spends more
completely over time. The non-crosslinked spent acid can then be flowed back
from the formation with relative ease.
Acid solubility test for 15% HCl and crosslinked acid was performed to design
the acid job and the result showed that Senoro carbonate has 90% solubility.
This crosslinked acid serves as a diversion agent that will facilitate the acid
to be evenly distributed along the interest zone. The well test result before
stimulation was 13 MMSCFD gas with skin value of +3 (obtained from PBU test),
while permeability was 4 md. The well was tested again after stimulation.
Significant increased gas rate was observed while the skin damage
decreased.
This paper describes the planning and implementation of crosslinked acid
application as an effective diversion agent in long interval matrix acidizing
stimulation. Furthermore, it explains the criteria to determine the efficiency
of this application.
Introduction
Well-S located at Senoro Field, Senoro - Toili Block, Central Sulawesi,
which operates under concession of JOB Pertamina - Medco E&P Tomori
Sulawesi (JOB PMTS). Well-S is a delineation well drilled to confirm
gas/condensate reserves at the southern part of Senoro - Toili structure
This well is a directional well with 7100-ft MD of total depth and 32o of
maximum inclination and penetrates Senoro structure – anticline structure with
a large gas trap. Reservoir target of this well is Minahaki formation which was
successfully penetrated.
DST is used to test Minahaki formation with perforation length of 75-ft using
TCP gun. Matrix acidizing was chosen to be the stimulation technique, but a
quite long perforation length being an obvious challenge for stimulation. The
well then being temporary abandoned after stimulated and re-tested for future
development scenario.
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